After we verified the leak was fixed we started the reassembly process. The block face was cleaned then the head gasket was positioned and set dry.
The head was also cleaned and prepared for installation.
Because the push rods and rocker arms were not removed from the head, it was decided to apply torque in stages so as not to damage the push rods. Tool tight was followed by 25, 50, then the full 65 foot pounds of torque.
Before installing the intake plenum, high temperature blue silicone was used around all the water ports. This is insurance beyond the standard intake gaskets. In this picture you can see the blue silicone applied in two places on the right head. The second intake gasket was installed immediately after this picture was taken.
The plenum was set then torqued to 35 foot pounds.
The fuel filter, distributor, coil, plug wires and hangers were all reinstalled.
It took a lot of work to fix this oil leak but we did get to see the internals of our 327. All-in-all it wasn't that bad.
Now it's time to focus on the fuel injection unit.